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The flight controller using 4.5.0 firmware has high noise with gyro
To Reproduce
1.cloud build 4.5.0 TMTR-TMOTORVELOXF7SE target,and flash to FC
2.start to fly
3.into cli and enter:
resource MOTOR 5 NONE
resource MOTOR 6 NONE
resource MOTOR 7 NONE
resource MOTOR 8 NONE
resource MOTOR 5 C08
resource MOTOR 6 C09
resource MOTOR 7 A08
resource MOTOR 8 A09
save
4.start to fly
Expected behavior
Two flight will have same gyro noisy,but actually there are dirffrent.
Support ID
1a16c0ee-2423-493e-8ce7-0c1cd11f092b
Flight controller
TMOTOR Velox F7 SE
Other components
RX:ELRS 3.0 receiever
VTX:analog
ESC:V50A SE
How are the different components wired up (including port information)
RX:UART3
VTX:UART2
ESC:MOTOR1-MOTOR4
Add any other context about the problem that you think might be relevant here
No response
The text was updated successfully, but these errors were encountered:
The flight controller using 4.5.0 firmware has high noise with gyro
To Reproduce
1.cloud build 4.5.0 TMTR-TMOTORVELOXF7SE target,and flash to FC 2.start to fly 3.into cli and enter:
resource MOTOR 5 NONE
resource MOTOR 6 NONE
resource MOTOR 7 NONE
resource MOTOR 8 NONE
resource MOTOR 5 C08
resource MOTOR 6 C09
resource MOTOR 7 A08
resource MOTOR 8 A09
save
4.start to fly
Expected behavior
Two flight will have same gyro noisy,but actually there are dirffrent.
Support ID
1a16c0ee-2423-493e-8ce7-0c1cd11f092b
Flight controller
TMOTOR Velox F7 SE
Other components
RX:ELRS 3.0 receiever VTX:analog ESC:V50A SE
How are the different components wired up (including port information)
RX:UART3 VTX:UART2 ESC:MOTOR1-MOTOR4
Add any other context about the problem that you think might be relevant here
No response
please can you provide a log and a backup of the setup (from preset page)
Describe the bug
The flight controller using 4.5.0 firmware has high noise with gyro
To Reproduce
1.cloud build 4.5.0 TMTR-TMOTORVELOXF7SE target,and flash to FC
2.start to fly
3.into cli and enter:
4.start to fly
Expected behavior
Two flight will have same gyro noisy,but actually there are dirffrent.
Support ID
Flight controller
TMOTOR Velox F7 SE
Other components
RX:ELRS 3.0 receiever
VTX:analog
ESC:V50A SE
How are the different components wired up (including port information)
RX:UART3
VTX:UART2
ESC:MOTOR1-MOTOR4
Add any other context about the problem that you think might be relevant here
No response
The text was updated successfully, but these errors were encountered: