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Aborted (core dumped) #1

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bharath5673 opened this issue Sep 27, 2021 · 1 comment
Closed

Aborted (core dumped) #1

bharath5673 opened this issue Sep 27, 2021 · 1 comment

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@bharath5673
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(depthai-test) bharath@nitro:~/Desktop/PROJECTS/depthai_projects/vision_ui$ python3 main.py 
pygame 2.0.1 (SDL 2.0.14, Python 3.9.7)
Hello from the pygame community. https://www.pygame.org/contribute.html
Palm detection blob : /home/bharath/Desktop/PROJECTS/depthai_projects/vision_ui/ai_models/palm_detection_sh4.blob
Landmark blob       : /home/bharath/Desktop/PROJECTS/depthai_projects/vision_ui/ai_models/hand_landmark_sh4.blob
[14442C10917AC8D200] [199.826] [system] [info] PRINT:LeonCss: BootloaderConfig.options1 checksum doesn't match. Is: 0x102C4414 should be: 0xAED890DB
BootloaderConfig.options2 checksum doesn't match. Is: 0x00000000 should be: 0x2380F205
GPIO boot mode 0x16, interface USBD
Setting aons(0..4) back to boot from flash (offset = 0)
====ENABLE WATCHDOG====1
--> brdInit ...
initial keepalive, countdown: 10
PLL0: 700000 AUX_IO0: 24000 AUX_IO1: 24000 MCFG: 24000 MECFG: 24000
Board init ret 3
brdInitAuxDevices: Error: SC = 27: io_initialize expander_cam_gpios_1 [OK]

spi_N25Q_init: Flash JEDEC ID: ff ff ff
eeprom_read_status 0!
EEPROM read status 0
EEPROM data version: 5
Closing EEPROm!
Is booted from flash by bootloader: 0
Networking not available...
Called by: LOS, controller: LOS
Enumerating on socket: Cam_A / RGB / Center
IMX378 patch for VCM type
  >> Registered camera A12N02A (imx378) as /dev/Camera_0
Enumerating on socket: Cam_B / Left
  >> Registered camera TG161B (ov9282) as /dev/Camera_1
Enumerating on socket: Cam_C / Right
  >> Registered camera TG161B (ov9282) as /dev/Camera_2
Enumerating on socket: CAM_D
Initializing XLink...
UsbPumpVscAppI_Event: 5 VSC2_EVENT_ATTACH
UsbPumpVscAppI_Event: 2 VSC2_EVENT_SUSPEND
UsbPumpVscAppI_Event: 3 VSC2_EVENT_RESUME
UsbPumpVscAppI_Event: 4 VSC2_EVENT_RESET
initial keepalive, countdown: 9
UsbPumpVscAppI_Event: 4 VSC2_EVENT_RESET
UsbPumpVscAppI_Event: 4 VSC2_EVENT_RESET
UsbPumpVscAppI_Event: 4 VSC2_EVENT_RESET
UsbPumpVscAppI_Event: 2 VSC2_EVENT_SUSPEND
UsbPumpVscAppI_Event: 3 VSC2_EVENT_RESUME
UsbPumpVscAppI_Event: 0 VSC2_EVENT_INTERFACE_UP
UsbPumpVscAppI_Event: 2 VSC2_EVENT_SUSPEND
UsbPumpVscAppI_Event: 3 VSC2_EVENT_RESUME
Done!
Usb connection speed: High - USB 2.0
I: [Timesync] [   1019244] [main] startSync:116     Timesync | Callback not set
Temperature: Driver registered.
Temperature: Initialized driver.
Temperature: Sensor opened: CSS.
Temperature: Sensor opened: MSS.
Temperature: Sensor opened: UPA.
Temperature: Sensor opened: DSS.
[14442C10917AC8D200] [199.826] [system] [info] PRINT:LeonMss: Called by: LRT, controller: LOS
Internal camera FPS set to: 23
Sensor resolution: (1920, 1080)
Internal camera image size: 1152 x 648 - crop_w:0 pad_h: 252
896 anchors have been created
Creating pipeline...
Creating Color Camera...
Creating Palm Detection Neural Network...
Creating Hand Landmark Neural Network...
Pipeline created.
terminate called without an active exception
Stack trace (most recent call last):
#29   Object "[0xffffffffffffffff]", at 0xffffffffffffffff, in 
#28   Object "python3", at 0x555f061d1bc2, in 
#27   Object "/lib/x86_64-linux-gnu/libc.so.6", at 0x7fadc0bd80b2, in __libc_start_main
#26   Object "python3", at 0x555f0624cd78, in Py_BytesMain
#25   Object "python3", at 0x555f0624cc7e, in Py_RunMain
#24   Object "python3", at 0x555f0624c49e, in PyRun_SimpleFileExFlags
#23   Object "python3", at 0x555f060ec60c, in 
#22   Object "python3", at 0x555f06247704, in 
#21   Object "python3", at 0x555f06213c5a, in 
#20   Object "python3", at 0x555f061629ea, in PyEval_EvalCode
#19   Object "python3", at 0x555f06213bab, in PyEval_EvalCodeEx
#18   Object "python3", at 0x555f061618e1, in 
#17   Object "python3", at 0x555f061aa852, in _PyEval_EvalFrameDefault
#16   Object "python3", at 0x555f061239ba, in _PyObject_MakeTpCall
#15   Object "python3", at 0x555f0615d3d8, in 
#14   Object "python3", at 0x555f0615384d, in _PyObject_FastCallDictTstate
#13   Object "python3", at 0x555f06162526, in _PyFunction_Vectorcall
#12   Object "python3", at 0x555f061618e1, in 
#11   Object "python3", at 0x555f060d8fdb, in 
#10   Object "python3", at 0x555f060b4e18, in 
#9    Object "python3", at 0x555f061239ee, in _PyObject_MakeTpCall
#8    Object "python3", at 0x555f06153713, in 
#7    Object "/home/bharath/anaconda3/envs/depthai-test/lib/python3.9/site-packages/depthai.cpython-39-x86_64-linux-gnu.so", at 0x7fad98ac3a6e, in 
#6    Object "/home/bharath/anaconda3/envs/depthai-test/lib/python3.9/site-packages/depthai.cpython-39-x86_64-linux-gnu.so", at 0x7fad98adef92, in 
#5    Object "/home/bharath/anaconda3/envs/depthai-test/lib/python3.9/site-packages/depthai.cpython-39-x86_64-linux-gnu.so", at 0x7fad98c24cc3, in dai::DeviceBase::startPipelineImpl(dai::Pipeline const&)
#4    Object "/home/bharath/anaconda3/envs/depthai-test/bin/../lib/libstdc++.so.6", at 0x7fadb7944fb0, in std::terminate()
#3    Object "/home/bharath/anaconda3/envs/depthai-test/bin/../lib/libstdc++.so.6", at 0x7fadb7944f6e, in 
#2    Object "/home/bharath/anaconda3/envs/depthai-test/bin/../lib/libstdc++.so.6", at 0x7fadb7946871, in __gnu_cxx::__verbose_terminate_handler()
#1    Object "/lib/x86_64-linux-gnu/libc.so.6", at 0x7fadc0bd6858, in abort
#0    Object "/lib/x86_64-linux-gnu/libc.so.6", at 0x7fadc0bf718b, in gsignal
Aborted (Signal sent by tkill() 4125 1000)
Aborted (core dumped)

unable to run please help...:((

my env specs:
Python 3.9.7 (default, Sep 16 2021, 13:09:58)
[GCC 7.5.0] :: Anaconda, Inc. on linux

@michaelhwn
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Hi, may I know which hardware (is it OKA-D?) you are trying to run the project on? The error "BootloaderConfig.options2 checksum doesn't match" seems an indication that the problem may be a hardware/firmware-related issue.

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