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CAN Error: Check Connections #4

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ConnorBarthet opened this issue May 16, 2021 · 10 comments
Open

CAN Error: Check Connections #4

ConnorBarthet opened this issue May 16, 2021 · 10 comments

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@ConnorBarthet
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Connections are fine but the device gives the error listed above. The device is getting information from my car such as the brakes, so I know it is communication on some level, but I cannot engage OP.

@oricalworks
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More information please like what car and type of harness? and did u just get op? Is vanilla working?

@oricalworks
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Videos are helpful. Try to provide as much information as possible please

@ConnorBarthet
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image

@ConnorBarthet
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2019 Hyundai Santa Fe Limited
Hyundai D Harness
Vanilla works fine
This is my first time trying this fork. I installed using: git remote add neokii https://github.com/neokii/op4.git && git fetch --all && git checkout hkg_084_dev

@oricalworks
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Latest 085 update still has his car broken. Any ideas?

@neokii
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neokii commented May 20, 2021

Turn off long control in the settings.
Settings -> Community -> Turn off "Enable HKG Long Control"

If scc is on bus 0, long control does not work.

@ConnorBarthet
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Long Control does work. It works on this fork:
https://github.com/andy741217/dragonpilot

@ConnorBarthet
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But it is only vision long. Orical and I think it has something to do with the radar.

@ConnorBarthet
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The latest update did not fix the issue. CAN Error: Check Connections still present

@oricalworks
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oricalworks commented May 25, 2021

His car works on OpenPilot long without moving scc off of bus 0 to 2 on this fork
https://github.com/andy741217/dragonpilot

oricalworks referenced this issue in Circuit-Pro/openpilot Jun 6, 2021
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3 participants