Skip to content
New issue

Have a question about this project? Sign up for a free GitHub account to open an issue and contact its maintainers and the community.

By clicking “Sign up for GitHub”, you agree to our terms of service and privacy statement. We’ll occasionally send you account related emails.

Already on GitHub? Sign in to your account

Fix: Inav 7.0.0 last build not working on SPEEDYBEEF405V3 #9162

Merged
merged 1 commit into from Jul 12, 2023

Conversation

shirase
Copy link
Contributor

@shirase shirase commented Jul 6, 2023

Bug appears if you use analog OSD on SPEEDYBEEF405V3 and do not insert sd card.
SD card try to initialise many times and eche time slow down SPI bus speed, but analog OSD works on same SPI bus. When spi slow down, analog OSD slow and increase pid loop. It make unstabile gyro calibration. That fix restore standard bus speed after first attempt.
Fix #9153

@DzikuVx DzikuVx added this to the 7.0 milestone Jul 7, 2023
@DzikuVx
Copy link
Member

DzikuVx commented Jul 7, 2023

Awesome, thank you very much @shirase

@DzikuVx DzikuVx merged commit 15beb67 into iNavFlight:master Jul 12, 2023
14 checks passed
Sign up for free to join this conversation on GitHub. Already have an account? Sign in to comment
Labels
None yet
Projects
None yet
Development

Successfully merging this pull request may close these issues.

Inav 7.0.0 last build not working on SPEEDYBEEF405V3
2 participants