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Description
With the current release (actually current code as well) as has been mentioned on a few threads now including:
https://forum.arduino.cc/t/serial-print-from-isr-will-hang/1145292
If you run a sketch like the unmodified example RTC->Test_RTC
The program will completely hang when it tries to do any Serial.print() statements... Actually would be true as well for Serial1.print()...
I am guessing that the current UART class code has not really been completed but just enough to be able to use the new board.
For example I am assuming that at some point there will be a TX software queue and the like.
But a quick and dirty fix would be to change the Interrupt priority for the UART to a high enough priority such that the NVIC code would allow it to be called from for example a timer interrupt callback.
On my machine I changed cores\arduino\IRQManager.cpp: line 14:
#define UART_SCI_PRIORITY 6 //12
Which allows it to preempt most IRQs except maybe SPI Master.
But again I do not believe this should be the long term fix, but may be sufficient for the short term
Edit: Note I have the Uno R4 Wifi